High Bright News Print Qualifying Trial
Stock
- 43# High Bright News Print
- Roll #1 - D5Y192151D
- Roll #2 - D5Y192151E
Graphics
- 4 color process / 2 color
- 100 line screen halftones both color and B / W
- Various text with some large solids and screen tints.
Plates
CTP from existing in house files.
Press
- 985 (reconditioned) Goss Community
- 35” heatset with 3 print towers and 3 chills per tower.
- Prints blanket to blanket.
Water system
Integrated
Registration Control
RGS V auto register system.
Manual ink control. Ink fountains fed from central tote system.
Speed
Normal operating speed – 25,000 IPH
Trial run speed – 25,000 IPH
Roll Stand - 2 - Butler dbl web roll stands.
Press Set-Up - Middle 4 / Color Tower Used
- 1st unit – Cyan
- 2nd unit – Black
- 3rd unit – Magenta
- 4th unit – Process yellow
Infeed
No nip pressure at web guide with chill speed set at + 0.092.
Blanket cylinders - Packed N/A
Plate cylinders - Packed N/A
Ink – Flint Ink - uni-tack
Ink tack - Process black – 5
Cyan - 5
Magenta - 5
Process yellow – 5
Densitometer - N/A
Fountain Solution
- Rycoline concentrate manually mixed by crew.
- pH of 3.5 and conductivity of 2000 using city water.
- Stand alone recalculating tank.
Blankets
Compressible .067 thicknesses.
Run Temperatures
- Oven temp 250 deg.
- Chill roll temp 50 deg.
- Fountain solution 65 deg.
Observations
Press appears to be well maintained and all settings, pressures and temperatures are within normal operating specs.
Both test rolls looked to be in good condition and were still wrapped just prior to the press run.
Print trial started at 10:am. Roll #1 pulled up with no problems and the crew dialed in fit and register along with color balance at a make ready speed of 15,000 IPH. After about 7000 cutoffs of roll #1, the pressman informed me that he was ready. I made some minor color moves to balance color and marked the first pull sheet as #1. This sheet was used as our color sample to maintain consistent color throughout the run. . Press speed was increased to 25,000 IPH for the balance of the test. The balance of roll #1 ran well with no problems and sample sheets were pulled about every 1000 cutoffs. No significant dusting was visible on the print unit blankets.
Roll #2 experienced a missed splice that was determined to be operator error and not paper related. The press was re-webbed and roll #2 pulled up with no issues. Color and register was maintained throughout roll #2 with no issues. The press was stopped about 1/3 way through the 2nd roll to change a bad water metering roller on the yellow unit which took about 10 minutes. The press was started back up with no issues. The 2nd roll was run completely out with sample being pulled about every 1000 cutoffs. Blankets on all 4 units were closely inspected after the run. No significant dusting was seen on any of the blankets.
Consultant Comments
Paper ran very good with no infeed, running, print, drying or folding issues. No significant dusting was seen even after 2 full rolls were run. No hickies were seen in any of the solid areas of the print graphics through out the entire run. The pressman commented that the paper ran as clean as or cleaner than what he normally sees on similar paper. No web guide or register issues were seen during the run.
To see the resume of the expert associated with this case study, see the link below.
| Resume of BMP | Commercial Printing, Paper Manufacturing, Expert Consultant Resume |